Has very loud ticking noise, #5 was not firing. I took the drivers side valve off to find #5 intake valve not seated in the up/closed position. Put compressed air in through spark plug hole, air was blowing out throttle body. I guess the valve somehow contacted the piston and bent. I tried prying the valve closed but it would not close completely with rocker arm off. The push rod was straight and appeared to be good shape. Could a failed lifter do this or what? I have been researching reman long block, any advise? Fraser reman engine is close by...