Dantheman1540
Full Access Member
Played with the tune and got it to sound more aggressive without making the engine run like it's missing cylinders. It still wants to drop to far after a high rev so I need to figure that out but it's very driveable and WOT safe now.
I went ahead and ordered a Magnaflow 12599 muffler and hopefully I'll have that in soonish.
Heres some questions I asked myself before I started this and the now found answers.
Question: Does the truck feel faster?
Answer: No not really. I do feel that it continues to pull harder after 5500 up to 6500 but I don't believe it is anymore than a 1/10sec or so faster in the 1/4 mile.
Q: Did it lose low end.
A: Feels no difference down low. It still puts you back in your in your seat in 1st and 2nd gear. However my gear ratios are similar to the NNBS 6 speed guys so 4l60 guys you would probably notice it sluggish off the line.
Q: Any other benefits?
A: The valve train is considerably quieter. Could have been a minor exhaust leak that is fixed or possibly dual valve springs and the CHE trunion upgrade make for less noise.
Q: What would I do different?
A: Given more time I would have gotten some custom heads or had these sent off for CNC porting. Also would have gotten custom head gasket to raise comp ratio closer to 11-1. It's at 10.4-1 now. Even with those upgrades I doubt it would pickup more than 10% power gains.
Since I like posting terrible videos heres another one where it pathetically dies after a rev
I went ahead and ordered a Magnaflow 12599 muffler and hopefully I'll have that in soonish.
Heres some questions I asked myself before I started this and the now found answers.
Question: Does the truck feel faster?
Answer: No not really. I do feel that it continues to pull harder after 5500 up to 6500 but I don't believe it is anymore than a 1/10sec or so faster in the 1/4 mile.
Q: Did it lose low end.
A: Feels no difference down low. It still puts you back in your in your seat in 1st and 2nd gear. However my gear ratios are similar to the NNBS 6 speed guys so 4l60 guys you would probably notice it sluggish off the line.
Q: Any other benefits?
A: The valve train is considerably quieter. Could have been a minor exhaust leak that is fixed or possibly dual valve springs and the CHE trunion upgrade make for less noise.
Q: What would I do different?
A: Given more time I would have gotten some custom heads or had these sent off for CNC porting. Also would have gotten custom head gasket to raise comp ratio closer to 11-1. It's at 10.4-1 now. Even with those upgrades I doubt it would pickup more than 10% power gains.
Since I like posting terrible videos heres another one where it pathetically dies after a rev