nickbeckss
TYF Newbie
- Joined
- Sep 3, 2017
- Posts
- 9
- Reaction score
- 2
Well the truck spent the week at the service department (dropped off Monday, picked up Friday)... swathdiver you were pretty dead on. Their experienced tech (40+ yrs per the Service Manager) was tasked with tracking down the cause of "excessive voltage drop" that was identified at the fuel level sensor. They traced it back to a connector where the gas tank harness connects into the main body harness near one of the shock towers (service documents indicate: Installed 19119842 : SL-N-WIRE (08965-BOPCK) 19119, Replaced the Harness Connector at X125). Hopefully that's the end of my issues.
Curious if any of you with technical document access have any details on the items and locations of the replacement 19119842, 08965-BOPCK, 19119 or X125??
Also regarding the homelink... they did a test with a J41540 Transceiver Tester and found that module to be bad and also replaced that.
Curious if any of you with technical document access have any details on the items and locations of the replacement 19119842, 08965-BOPCK, 19119 or X125??
Also regarding the homelink... they did a test with a J41540 Transceiver Tester and found that module to be bad and also replaced that.