Tiredmechanic23
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- Joined
- Sep 19, 2019
- Posts
- 198
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- 137
So back 3 years or so ago and 90K miles ago my stock converter did its thing and took a crap and I lost everything but 1st and 2nd. Now I have a full built trans from TK performance and a billet 4 carbon fiber clutch converter that I have really beat on for the last 90K miles. The tahoe has a TCM and engine tune via Blackbear and a autocal. It has other minor engine mods which they tuned for. I drive this thing like a vette most of the time and have hurt feelings when I can and still trusted it to go anywhere. As of last week though it started randomly throwing a CEL and losing lockup in 6th. Id be cruising uphill on the highway at say 60mph and you would feel the trans give a slight hicup and the rpms would jump to about 3k and id get a CEL. Codes was always for converter clutch stuck open (P0741) if I remember correctly. Everytime it happened I could clear the code and continue on my way. Then randomly the trans developed a light whine. This entire time it shifted 1-6 just fine with no slip no matter the load. Suddenly though today while driving home from my sons practice while running about 60mph there was a hicup from the trans then it was all neutral except for park and the whine is much much louder.
Onto a few important details. When the first failure happend on the stock setup the pan was full of gold and it was a converter only failure and 1st and 2nd were the only gears I had besides reverse. TKPerformance confirmed this up on teardown and offered to refund me the build price and just charge to do a cleanout as the clutches and all were fine in the trans itself. I opted to build for performance though as I had mods planned out. This built was the max tier build from TK performance minus the billet planetary option as im not doing launches on a prepped track. It was paired with a PATC converter at 2k stall part "PQ80" on their site. Its a 10 inch billet hand welded converter with 4 carbon fiber clutches. At the time it was the best you could buy for this trans. Its had service done every 30k with filter and fluid. The most recent service was about a month ago and the pan was clean and the fluid looked good and smelled fine. The filter did have some gold in it though making think I had some converter wear going on but I had no signs of issues so was hoping/thinking id be ok still for a bit but to just not be so rough on it for now. I called the converter company (PATC) and asked if they could rebuild/refresh it if need be and planned to have them do so when I could down the vehicle hopefully after Xmas.
I can get a cheap reman POS converter to get by on to get to work and back for 300 or less and putt around while I get my nice converter redone. Of course there are cost in a cooler and new filter and fluids and trans clean out but it would get by for a bit.
So whats everyones opinion? Converter took a dump or do we think the trans is dead? Even if its just the converter I plan to get the trans cleaned out and swap to a new cooler again to prevent trash getting into it after repair.
Onto a few important details. When the first failure happend on the stock setup the pan was full of gold and it was a converter only failure and 1st and 2nd were the only gears I had besides reverse. TKPerformance confirmed this up on teardown and offered to refund me the build price and just charge to do a cleanout as the clutches and all were fine in the trans itself. I opted to build for performance though as I had mods planned out. This built was the max tier build from TK performance minus the billet planetary option as im not doing launches on a prepped track. It was paired with a PATC converter at 2k stall part "PQ80" on their site. Its a 10 inch billet hand welded converter with 4 carbon fiber clutches. At the time it was the best you could buy for this trans. Its had service done every 30k with filter and fluid. The most recent service was about a month ago and the pan was clean and the fluid looked good and smelled fine. The filter did have some gold in it though making think I had some converter wear going on but I had no signs of issues so was hoping/thinking id be ok still for a bit but to just not be so rough on it for now. I called the converter company (PATC) and asked if they could rebuild/refresh it if need be and planned to have them do so when I could down the vehicle hopefully after Xmas.
I can get a cheap reman POS converter to get by on to get to work and back for 300 or less and putt around while I get my nice converter redone. Of course there are cost in a cooler and new filter and fluids and trans clean out but it would get by for a bit.
So whats everyones opinion? Converter took a dump or do we think the trans is dead? Even if its just the converter I plan to get the trans cleaned out and swap to a new cooler again to prevent trash getting into it after repair.