randeez
Full Access Member
turned it up and promptly broke something
what i thought was going to be a little turn up on boost controller.... was a whole bunch.
on top of that I figured it was going to be a lot lazier but turbo lit off and boost shot up to like 250kpa absolute on log (250-101)/6.9=21.5 psi (101kpa=atmosphere) from a roll this was only like 60%tps @4500rpm
got out of it quick, stopped soon as i could and closed up the controller (back to wastegate) everything seemed pretty good, was a few miles from house, kept looking over a few things on the way back everything good and just normal driving started making some clacking sound it sounded like top end valve train, figured a rocker or spring or something busted. limped it home. sat on it a few days and didnt feel like messing with it. started up it was hard to pinpoint from where it was coming sounded like back of engine but couldnt really tell which side.
pulled valve covers thursday, everything was pretty tight passengerside cyl 6/8 the lash on the rockers was kinda loose springs were tight but thought it was odd even while turning engine over but o well definitely dont think that was the issue, crawled under and looked at flexplate best i could (have new one waiting to go on) but not so sure thats it either.
soooo started pulling engine friday night pretty much just took off the downpipe and turbo. today friend and i ran over to my brothers to grab engine hoist and stand, messed around most of the day doin family crap didnt get back to it till about 4 this afternoon, another couple hours tomorrow and it should be out
it still starts up and idles fine sounds like its running on 8 cyls ive got a whole list of stuff ive wanted to get to so hopefully i dont have to do something with engine at the moment
what i thought was going to be a little turn up on boost controller.... was a whole bunch.
on top of that I figured it was going to be a lot lazier but turbo lit off and boost shot up to like 250kpa absolute on log (250-101)/6.9=21.5 psi (101kpa=atmosphere) from a roll this was only like 60%tps @4500rpm
got out of it quick, stopped soon as i could and closed up the controller (back to wastegate) everything seemed pretty good, was a few miles from house, kept looking over a few things on the way back everything good and just normal driving started making some clacking sound it sounded like top end valve train, figured a rocker or spring or something busted. limped it home. sat on it a few days and didnt feel like messing with it. started up it was hard to pinpoint from where it was coming sounded like back of engine but couldnt really tell which side.
pulled valve covers thursday, everything was pretty tight passengerside cyl 6/8 the lash on the rockers was kinda loose springs were tight but thought it was odd even while turning engine over but o well definitely dont think that was the issue, crawled under and looked at flexplate best i could (have new one waiting to go on) but not so sure thats it either.
soooo started pulling engine friday night pretty much just took off the downpipe and turbo. today friend and i ran over to my brothers to grab engine hoist and stand, messed around most of the day doin family crap didnt get back to it till about 4 this afternoon, another couple hours tomorrow and it should be out
it still starts up and idles fine sounds like its running on 8 cyls ive got a whole list of stuff ive wanted to get to so hopefully i dont have to do something with engine at the moment