07marmalade
TYF Newbie
- Joined
- Apr 19, 2010
- Posts
- 19
- Reaction score
- 0
Last night I bought a can of seafoam from autozone. I've done it to many of my previous cars before (around 5) but I thought when I did it to the escalade w/ 71.5k miles, it was a bit wierd.
I Unplugged the brake booster line and started her up. Like usual, it seems like its going to stall. I pour maybe 200mL into a cup for the booster to suck it up. I have my friend on the throttle. It sucks it up and the motor revs by itself (i thought it was my buddy but the whole time his foot was off the throttle). Halfway in the starts to knock, not the regular tick tick tick knock but a very loud explosion knock. Sounding like I was doing some damage. The engine was shaking bad in the mounts. I tell my friend to quickly shut her down to prevent any damage. The engine was still running for 3-5 seconds after he pulled the key out (wierd). A good amount of smoke is already out of the tail pipe. Wait for 15 minutes.
Start it up, not much smoke, not much more than a cold winter day. Drive around with some high revs. No codes. An hour later, my friend and I think that we didn't put enough since it's a 6.2L. Same process except this time it maybe sucked 50mL before it stalled. There was also a "service traction control" and also "service stabiltrak" error on the dash screen. Wait 15 min, start it up, no smoke. Drove around with really abrupt shifts.
I disconnected the battery for a few hours and seemed to wipe the service messages. I'm about to change the plugs now.
Anyone else experience this?
I Unplugged the brake booster line and started her up. Like usual, it seems like its going to stall. I pour maybe 200mL into a cup for the booster to suck it up. I have my friend on the throttle. It sucks it up and the motor revs by itself (i thought it was my buddy but the whole time his foot was off the throttle). Halfway in the starts to knock, not the regular tick tick tick knock but a very loud explosion knock. Sounding like I was doing some damage. The engine was shaking bad in the mounts. I tell my friend to quickly shut her down to prevent any damage. The engine was still running for 3-5 seconds after he pulled the key out (wierd). A good amount of smoke is already out of the tail pipe. Wait for 15 minutes.
Start it up, not much smoke, not much more than a cold winter day. Drive around with some high revs. No codes. An hour later, my friend and I think that we didn't put enough since it's a 6.2L. Same process except this time it maybe sucked 50mL before it stalled. There was also a "service traction control" and also "service stabiltrak" error on the dash screen. Wait 15 min, start it up, no smoke. Drove around with really abrupt shifts.
I disconnected the battery for a few hours and seemed to wipe the service messages. I'm about to change the plugs now.
Anyone else experience this?