Slowly working on the hoe still.
Last night I re-named her to Hoemare.
Nightmare + Hoe
(Pronounced Hoenir once issues have been sorted)
During my test drives with the line pressure gauges, i started noticing what felt like looseness in the alignment.
When pulling the wheels, i felt it
Probably a loose ball joint.
Didn't look at it too hard, but it just made the list of things to do.
After the engine and transmission issues have been taken care of.
I also made a slight mistake when placing the hoe in the garage.
I was trying to push it back and to the side of the garage to give me max space in there.
Since I'm planning to tackle the engine and transmission together, I need more space.
Got the hoe too close to the back of the garage.
I have my old craftsman toolbox behind it.
And there was a drill press next to that.
Hitch was touching the drill press and was binding on the bumper as i tried to jack the Hoemare up.
So i crawled under the back and pushed that took box back.
And managed to get the drill press on it's side.
Lucky!!
Last night,
Removed front axle to make things easier
(+ I'm fkn good at it now... lol )
Got all cooler lines free.
All electrical disconnected and clear of the engine.
Oil Cooler lines all disconnected but not fully removed.
Starter removed
Decided to yank the passenger side transmission mount this time.
Much easier with it off.
Found that it can trap water in the bolts from the top!!
Got some pretty black crap right in my eye.
Spent some time flushing that crud out... lol
When this goes back together, I'll seal the top of that bolt up...
That water has been in there for quite some time.
The hoe has not driven in and has not had the under hood cleaned since summer/early fall...
And the Intake is also Off
Figuring if i do end up tackling the engine to transmission bolts while it's up on jack stands, I don't want the intake to get pinned against the firewall.
Noticed some oil film in my pretty AFR intake ports.
Oil film is the wrong color.
Looks like the oil that I drained from the intake originally.
Also noticed some weird flakes.
almost looks like leftovers of the sparkles...
When I have the engine out, I'll bore scope each cylinder.
Might end up pulling the heads anyways, so i can assess...
I might end up replacing that intake for good measure either way.
Found it's about $200 +/- to replace with a new OEM unit.
I also purchased a proper lifting plate for an LS, since I'm planning to do this with the heads on this time around.
Got it nice and cheap as an amazon return.
but it's for a Gen 3.
Worked perfectly, just has a space in the back.
Taped off to prevent gunk from falling in....
Major tasks today, Pull the Y pipe.
Text my welder and tell him I'm ready to add that extra O2 bung.
Drain and recover Coolant.
Remove radiator and water pump.
Unbolt converter.
Then see if I get any further today...