2012 Suburban Misfire #5 drama

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Keiterburb

Keiterburb

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my 2010 had a strangely similar issue once, I'd circle back to that bundle of wires near the power steering pump. I've seen a few threads out there on the internet about those wires rubbing through and shorting, and the weird nature of this one feels very similar. Your P219A could also be indicative of an issue with that side's injector's harness. I'd get the pin outs to the ECM and ohm the connector from the injector harness to the ECM and with your meter connected I'm betting you will see the issue if you jiggle that harness by the power steering pump.
Will see about checking deeper into harness if I can find the schematic, shooting power and ground at injector harness and coil were solid? If I find connector and pins on ECM I could take off and shoot Ohm readings looking for jumping around when wiggling harness wear worn. Got noise light for injector plug coming in two days.
 
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Keiterburb

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Definitely looking up CASE relearn and checking if I have capability. I have had battery removed for long periods of time between maintenance, even tried throttle body relearn by cycling key on off 3 minutes on/60 off 3 times then idle for 5 min and drive cycle?? Don’t know if correct but following a video posted.
 
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Keiterburb

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I was able to figure out how to graph some data. Here’s is the O2 difference after 20 minutes on road and parked at idle. IMG_0628.jpegIMG_0630.jpeg
 

hagar

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Did you try swapping the number 5 injector to another hole? Wonder if the injector is over fueling based on those fuel trims?
 

j91z28d1

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that's removing a lot of fuel from bank one. you like the total to be around 5% long term + short term. you're at almost 20%.

now what's causing it, I don't know.
 
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Keiterburb

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Did you try swapping the number 5 injector to another hole? Wonder if the injector is over fueling based on those fuel trims?
All the injectors, plugs, and wires were replaced, gave a rundown of all the usual suspects have been swapped then replaced and am down to wiring other than what has been shot or internal failures
 
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Keiterburb

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that's removing a lot of fuel from bank one. you like the total to be around 5% long term + short term. you're at almost 20%.

now what's causing it, I don't know.
Could it be not enough intake valve opening due to cam lobe and pulling fuel? We may find out. I am waiting on a noid light and may be out of other options to check
 

j91z28d1

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Could it be not enough intake valve opening due to cam lobe and pulling fuel? We may find out. I am waiting on a noid light and may be out of other options to check
These things have kinda a noisey valve train at idle when not damaged. I'd be really surprised if you had valve train damage of some kind and it ran smooth and quiet.

but I'm also out of ideas. you'd done really good diagnostic at this point.
 

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